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       #Post#: 3473--------------------------------------------------
       Re: 175 design flaw part 1 of 2
       By: lynx wind Date: June 23, 2014, 2:49 pm
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       It is true the stator didn't come out perfect.  It was slightly
       thicker on one side.  Happens sometimes on the first try.  It
       had a 1/16" gap all around when it was adjusted which is
       typically a very safe gap.  On perfect alts this can be 1/32".
       I will adjust the stator parallel and adjust the gap between
       magnets and stator.  I will put as much torque on the speed nut
       as I can.  I have never had one come loose.
       Is it possible you are hearing the hum from the alternator as it
       makes power?  Or is it a definite clicking sound as something is
       striking against something?
       I will contact you about available times when I can pick up the
       alt.
       #Post#: 3474--------------------------------------------------
       Re: 175 design flaw part 1 of 2
       By: happygolucky Date: June 23, 2014, 6:24 pm
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       lynx  please do contact me either phone..it is  a  2 fold
       situation ...definite scratching sound as magnet plate is  plum
       an true we tightened   the nut!  magnet plate was  scraping
       surface ever so slight ,as i had mentioned...an pictures above
       on high side... the coupling that is pressed on the bottom is
       off also not plum on aluminum shaft  tilts the alternator/stator
       1/16th to 1/8 stack those too with stator thickness ... coupling
       add the over thickness from the resin  an it becomes an 1/8 or
       slightly more..i did extensive study an have experience in
       tolerance control... for many companies so parts would be within
       tolerance your tolerance is very tight 1/16th - 1/32 th  you can
       see the 2 slight marks in the photo above where the void
       is..where it was rubbing ..against magnet plate ...we caught it
       in time  an that is why i did not have good start up it was
       catching..i will show ...you/ i could sand it down  an make it
       true..on the high spots, but i am afraid of nicking wire
       removing to much material as it can be seen ... a Bridgeport
       with a   jig  an fixture would be ideal..
       the bottom is flat. the magnet plate is plum ...an perpendicular
       to to .25 thick magnet hihgth i did not check but assume are
       true on plate still do not know how the nut came loose..? or
       maybe just an over sight..
       i guess i could remove the thick part on stator/alteneator by
       sanding both parts or make a   metal shim from strapping
       material questionable idea but i  think that is the solution oil
       is leaking from bottom need a bead of caulk  to seal?.
       part 1 of 2
       #Post#: 3475--------------------------------------------------
       "Design Flaws Part 1 of 693"
       By: happygolucky Date: June 24, 2014, 8:00 am
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       duct tape over pole to take up play an make plum..inside of
       coupling on low side.  just a temporary fix..
       has anyone else run into this problem?
       very sloppy fit in coupling to emt pole should be snug fit ...
       like coupling over aluminum with 10 thousandths play  a snug
       slip  fit to coupling an emt  pole to remove play the 2 top set
       screws have no play...... even on the 160 gull as there any
       play..  a few ideas lynx ... a shim on the one side or sanding
       / filing.. the pole that is low/high on pole to remove material
       on pole to true an plum fit .....but then you still have rocking
       back an forth play.. ?  the top of pole since it rest on the
       bottom of stator an is double pinned with  2 )1/4 -20 bolts an
       lock washers would have to be re-drilled one it is made true an
       plum holes will be out of ligament .. i hope this is descriptive
       enough..
       stator must be square level an plum to 1 1/2" EMT POLE an then
       parallel to magnet plate.. that may be the reason for flicker in
       video when turning?
       this is just me  thinking solution threw,,..i will wait for your
       call an your solution.. i am home..
       HGL
       #Post#: 3476--------------------------------------------------
       Re: 175 design flaw part 1 of 2
       By: sut Date: June 24, 2014, 8:19 am
       ---------------------------------------------------------
       @ HGl what I have done and used to correct pole to coupling
       wobble is to use a piece of the same aluminum I used for wings .
       most of the time I just live with the slop and have not ran into
       any trouble
       #Post#: 3477--------------------------------------------------
       "Design Flaws Part 1 of 693"
       By: happygolucky Date: June 24, 2014, 9:08 am
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       sut
       in theory your correct... if everything is true an concentric
       on top but..... its just a another thing that i look at an am
       considering in this 175 kit ...in my new design shaft alignment
       will be critical in one of my applications ...no big deal, means
       nothing here i just thought i would mention it it drain
       water..really when it begins to spin it should true its self
       ,but the shaft will lean an wear on dia an cause friction. an
       transfer wobble eventually on one side oblong hole..take two
       motors an couple them together with shaft alignment... if one is
       out of alignment it wears on hub an bearings,  i tend to be to
       be to critical with tolerances.. they can get you into trouble..
       the other end of coupling on aluminum shaft, i see it is
       pressed on or epoxied off 1/8 the  2 set screws they are
       critical for holding.. my emt pipe sits on top the aluminum you
       do not want to see a slight lean know it may mean nothing in the
       175 but if true i believe it would start up in less wind?... now
       we are only talking a 1/6 -1/8th an inch that's for lynx to
       decide..
       all i do is observe an report..but i want to see my turbine
       working smooth as butter in the wind .
       thanks for the idea
       #Post#: 3486--------------------------------------------------
       Re: 175 design flaw part 1 of 2
       By: lynx wind Date: June 24, 2014, 7:38 pm
       ---------------------------------------------------------
       If oil is leaking from the bottom it is possible the adjustment
       nut was moved.  When installed it is put in with a locktite
       sealant.  I have never had one leak or move once set.  If it was
       readjusted the seal is broken and the hub has to be cleaned of
       oil, the magnet plate readjusted and the set screw put back in
       with locktite.  I leave this to dry overnite before lubing the
       hub.
       I would be happy to re-adjust this alternator for you.
       You sure have had some problems with this wind turbine!  Just
       about every component has been a challenging and frustrating
       experience.  I have learned a lot.
       #Post#: 3487--------------------------------------------------
       "Design Flaws Part 1 of 693"
       By: happygolucky Date: June 24, 2014, 8:37 pm
       ---------------------------------------------------------
       thank you..life is a challenge..i also have learned a lot..also.
       #Post#: 3489--------------------------------------------------
       Re: 175 design flaw part 1 of 2
       By: sut Date: June 25, 2014, 8:00 am
       ---------------------------------------------------------
       The only way you can remedy the coupling is to have it machined
       to fit the pipe then it adds cost to the kit . then you still
       are not guaranteed that a different manufacture of the same pipe
       would have the exact same size pipe
       #Post#: 3491--------------------------------------------------
       "Design Flaws Part 1 of 693"
       By: happygolucky Date: June 25, 2014, 10:21 am
       ---------------------------------------------------------
       all is all good sut,,minor glitches will happen its par for the
       course... i have full confidence in the 175 diy kit.. we are
       learning, as lynx proceeds forward ;D it goes with the process
       an territory ... i have told lynx every detail i analyze data an
       details... so that the 175 is an will be the finest vawt
       available for lynx an the team... i'm sure lynx will bring it to
       your attention as he is he team leader.... i'm documenting every
       detail even minor as it may be..some things may happen to your
       175 vawt i doubt it..i'm proud to be a team player an member..
       it is good to exchange data an information so that lynx is
       aware.
       it's  the little things that spoil the fox...
       HAPPY! :D
       #Post#: 3492--------------------------------------------------
       Re: 175 design flaw part 1 of 2
       By: lynx wind Date: June 25, 2014, 10:55 am
       ---------------------------------------------------------
       Happy and I made adjustments to the stator and readjusted the
       magnet plate.  Here is what I believe happened.
       It was clear the stator was not rock hard as you could see how
       when tightened the hub pushed into the urethane.  This caused
       the stator to be slightly cocked.  Evidently in the rush to get
       the alternator to happy the urethane was not fully cured.  We
       sanded the urethane to have a smooth seating surface to the hub,
       adjusted some more, adjusted the magnet plate.  It now runs true
       with about 3/32" gap.  RMS voltage at 60 rpm is about 7-8 volts
       ac
       The slight misalignment of the coupler to hub is due to the
       coupler not being a machined part.  In the future a machined hub
       that fits inside a 2" pipe will solve this and eliminate the
       need for an adaptor.
       I will probably go back to adding some fiberglass cloth in the
       center area of the stator and allow the stator to cure longer.
       That and a larger mounting surface with the larger hub will be
       improvements.
       I had hoped to produce more than one stator per day, but I think
       the stator should cure in the mold for 24 hours.
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