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       #Post#: 4044--------------------------------------------------
       Re: Seagull 175 Alternator
       By: lynx wind Date: August 4, 2014, 10:37 am
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       Yes, not a typo.  If you take two strands of 20 awg together in
       parallel it is equivalent to a single strand of 17 awg.  If you
       take four together in parallel it is equivalent to a single
       strand of 14 awg.
       The advantage to using smaller gauge in parallel is you can pack
       more in to the same space.  You can also output to separate
       connections which would give you options for 12, 24, 48 volts.
       You could up the turns to 55 and get more voltage, but achieving
       a lower cutin speed may not be wise if it occurs below tsr 1.0
       It might also be possible to use 19 awg instead of 20 awg and
       lower resistance even more.  I haven't tried that yet.
       #Post#: 4050--------------------------------------------------
       Re: Seagull 175 Alternator
       By: Otis Date: August 4, 2014, 7:39 pm
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       Sorry. My skull is pretty thick. So.. 100 turns of 15awg
       equivalent to is same as 50 turns of 14awg equivalent?seems like
       a big difference for one step of standard measurement scale. Or
       did you lower turns of 18awg to be used?
       #Post#: 4246--------------------------------------------------
       Re: Seagull 175 Alternator
       By: nessprojects Date: August 25, 2014, 5:14 pm
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       Been doing a little bench test with the alternator I received
       from Lynx....Connected a bridge and a 12v battery to the 12v
       terminals + Rpm meter.
       12v charge was reached at about 100 Rpm so I have a feeling this
       thing will not need a booster.
       #Post#: 4248--------------------------------------------------
       Re: Seagull 175 Alternator
       By: sut Date: August 26, 2014, 7:53 am
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       What do you use for rpm counter    is it your little raspberry
       #Post#: 4252--------------------------------------------------
       Re: Seagull 175 Alternator
       By: nessprojects Date: August 26, 2014, 5:05 pm
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       @sut
       Yeah I just couple up the arduino to the battery and 2 wires to
       the ac side of the alternator (It just has to sniff the
       frequency). I only hand wound the alternator just to get a idea
       of the 12v cut-in.
       #Post#: 4253--------------------------------------------------
       Re: Seagull 175 Alternator
       By: happygolucky Date: August 26, 2014, 5:28 pm
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       report 175 failure..  these are the facts!
       my  last report.... break dose not work on 175 alternator...
       just had 65-70 mph wind blow about the 4th or 5th storm this
       summer for about 5 min.. blew the 175 apart this time.... way to
       poor/ weak of a design to heavy...wrong pole not sturdy
       enough...it has  5 bolts in it now..aluminum airfoil sut blades
       twisted an separated opened right up like an envelope .019
       aluminum is to weak to use cannot take centrifugal force sorry
       sut..gave it a bloody good try.. separated at all seams using
       CG goop separated every where the weak link is the fiberglass
       rod gives to much bowing ,flexing an twisted apart.. goop glue
       did not hold up or stick to aluminum or wood ? top an bottom
       former's also failed  they split!!!!!!!!!! did see 150-175 watts
       you can do the math... before complete destruction..
       
       #Post#: 4254--------------------------------------------------
       Re: Seagull 175 Alternator
       By: happygolucky Date: August 26, 2014, 5:29 pm
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       2nd half of report..
       oh an rotor arms are bent down ward sagging started about 1 1/2
       months ago,  i should say warped.. a total failure!
       now the alternator is still blistered bubbling de-laminating an
       no brake like in video... i have great wind had been watch the
       former's and air foil  bulge, i snapped a pic an then took it
       down i thought i would wait.... it was from twisting was waiting
       for failure... i will now build it my way ...lasted the
       summer..would never have made it threw the winter.. what 3
       months?
       a heavy duty HAWT is in the making for back up as i Begin to
       redesign an build my new Vawt ...my solar has out preformed
       everything...already have the magnet in the 100 amp PMA
       alternator with neo magnets 500-1000 watts at 15-25 mph 80" wing
       span start up 2-3 mph- schedule 80 pipe not EMT slip collar with
       tie downs never build a wood rotor arms for VAWT..
       my advice has always been be honest truthful an fair.. ....use
       the best materials available you get what you pay for.. an do
       not cut corners..build it cheap you get cheap..
       hey CG you the big chief now... i only see your name..? same ole
       crow of a few..on board..
       hope you can do better..
       hgl
       #Post#: 4256--------------------------------------------------
       Re: Seagull 175 Alternator
       By: happygolucky Date: August 26, 2014, 8:20 pm
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       ps.. CG i bet you are ! no hard feelings just karma.... an a
       experiment that failed my beef was over bad  used GTI's  that
       are fixed now..
       i have a  many a spare vawt parts.... have some  made from
       aircraft aluminum, lighter etc.. also the steel shaft on magnet
       plate has some wear? or crust or galvanic corrosion or rubbing
       aluminum, i suspect it may have been rubbing inside alum hub
       hope it did not oblong ID should  bore an have ss sleeve pressed
       in alum hub  threaded at the bottom for set screw... it has been
       under a wind spin 80% of the time.. this summer. i have a nice
       dc-dc 400 watt buck booster..drives from 3v in  to  60v out with
       meter... going to use it in low wind applications.. this vawt
       will not do over 100 watt without failing.. as it was delivered
       an built.. your best is 50-75 watts on a good day 25 mph
       anything over an it will fail...
       after a complete tear down i examined  it further... a few of
       the magnets separated from the epoxy you used LYNX what was it?
       may just fill with epoxy resin an put in housing? very strange
       it was out of alignment with other magnet i tapped it back in
       line? what kind of epoxy did you use?...i like loctite on the
       magnet plate, paint is rustoleum  ... that magnet will have to
       be re-cemented  if  the slot was machined in  the magnet plate
       it would not move hint hint!
       i will make some changes an have another up an running...this
       week!
       #Post#: 4261--------------------------------------------------
       Re: Seagull 175 Alternator
       By: happygolucky Date: August 27, 2014, 10:53 am
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       well sut.. i have completely disassembled the 175 for further
       inspection.... nothing to salvage but magnet plate... i have to
       re epoxy a few magnets, spars an straps ok.. it's all in pieces
       wings bent an open as i described...but i can take pics of those
       parts... getting ready for a rebuild.. if the weather breaks..
       last night have some painting an redesign work to do... i did
       not save any pics sorry thought i did... the wife, son an
       neighbors  an myself are my only  witness.. did not save the
       earlier pic's either sorry, LYNX knew what was going to happen
       he said he was worried/afraid, quote un quote.. about it.... i
       saw what was happening too after his event.. i expected failure
       sorry that's physics......as far as balance it was balanced..
       but no breaking system it will not stop under wind load ..... an
       water did not penetrate any where until it opened up... it had
       no effect unless... while spinning at high speed  an driving
       rain maybe rain did beat on it adding more stress?sure was
       bending it was bending an bulging an twisting, we could see it
       happen i was watching.. it was sealed tight as a drum with
       silicone ..  to much stress under max wind conditions weak
       design links causing seam failure.. it started with a bulged at
       the former bottom an top  from fiber glass rod twisting an
       bending an then bent in the middle opening the seams... the rest
       is history.. sut... but i will see what i can do..
       #Post#: 4262--------------------------------------------------
       Re: Seagull 175 Alternator
       By: lynx wind Date: August 27, 2014, 11:05 am
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       This discussion is misplaced on this thread.  The topic is the
       Seagull 175 alternator.
       But to add on, the Seagull 175 that SUT and I built is doing
       great, rock solid and performing.  Just no 15+ mph winds in
       August except a few sporadic squalls.  Yesterday's brief squall
       had it working hard for about five minutes as the storm ran
       through.  Good winds come in the fall.  I am sure we will get
       good data from Nessprojects on performance and endurance.
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