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       #Post#: 2008--------------------------------------------------
       2ltr 8v Digifant power
       By: JMR Date: December 12, 2014, 9:34 am
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       We've done some work on Tim Hughes MK2 before, a lower F/D swap
       & a Quaife diff, along with a tailbox swap from the previous
       poor design which netted a 7hp peak power gain and 13hp (yep 1 &
       3!) gain at mid range peak torque rpm.
       
       Looking at the power curve the last time I saw the car, the way
       it levelled off between peak torque and peak power was telling
       me the engine was struggling to breathe as the revs rose. The
       engine was also down on power overall considering the spec (110
       at the wheels..133-134 at the flywheel), so my suggestion was I
       take a look at the head and see what we had to start with and
       look at improving the flow.
       
       The previous owner, a friend of Tim's, had an engine kit
       supplied and fitted along with, as we discovered, a 40.5 / 35mm
       head. I've always seen improvements with these with some re
       porting, but as we wanted to get the 2ltr breathing properly my
       suggestion was we kept with the 35mm exhaust valve but re port
       and add 42mm inlets. Now to cut a very long story short, as I
       opened the last inlet throat it cracked through...I've gone much
       bigger without an issue so this casting must have just been a
       bit thin, nothing my alloy welder guru cant fix...normally!
       
       After 3 attempts at grinding out and re welding it just wouldn't
       take as the pressure test showed...it can happen but its
       rare...so with time very much not on my side I started from
       scratch with another casting. Now we had a dilemma, or at least
       Tim did as I was confident I knew the answer. Tim had a budget
       (as we all do) to fit the bigger inlet valves & new inserts it
       needed as we were going to do on the original head, but bigger
       inserts to support the 35mm exhaust valves from the old head
       wasn't in the plan. It was simple in my head (pardon the pun!),
       we'll just use the 42mm inlets as intended but keep to the std
       33mm exhaust valves.
       
       Tim had some reservations about my 42 / 33 combo as the word on
       the street says a 2ltr needs a 35mm exhaust valve to make power.
       I politely pointed out that his name sakes (Tim Moll's) 2ltr
       race spec 8v crossflow made almost 200hp on 33mm exhaust valves
       so I wasn't too phased about hitting the target I wanted to see
       of around 150hp.
       While the head was off Tim measured the piston deck height for
       me so I could work out what needed skimming off the head to get
       the C.R right. It was then we discovered 2 more reasons for the
       engines lack of sparkle...the pistons were too far away from the
       block deck for decent squish, which in turn, along with the deep
       piston bowl, contributed to the C.R being roughly 1-1/2 points
       lower than ideal for the 276 cam used.
       With no perfect solution, I roughly closed the C.R deficit down
       by half by skimming the head as much as I dared with a view to
       maybe sorting the block at some point. The new 42 / 33 ported
       head was then sent back to Tim for re fitting, followed by the
       car heading back down to us to run up on the rollers for fine
       tweaking.
       However, at the end of the one and only power run, the rattle
       from the bottom end told me we would be looking at the rest of
       the engine sooner than planned! To cut another long story short,
       Tim left the car with us and returned a couple of weeks later to
       remove the engine for me to look inside. As I suspected, number
       3 big end had gone, resulting in a scrapped crank and rod.
       With a replacement crank found and some rods I had going spare
       that we fitted with ARP bolts, I re built the engine after
       correcting the squish & compression short fall while it was
       apart with a good skim of the block. After Tim returned to fit
       the engine, it fired up instantly for us to take straight over
       to the rollers to finish what we started once and for all. With
       time yet again not on our side, I bedded the rings and bearings
       in during the 5 mile drive to the rollers to see how much all
       the effort was worth....would we get close to our 150hp target,
       would we gain any more mid range?
       Well it certainly felt a bit stronger on the road, but with the
       ignition and fueling set at a conservative estimate I didn't
       push my luck too much. After some more running on the rollers
       and some basic setting up the fresh engine was much more
       responsive than the old, almost "open induction" like in
       throttle response...not bad for digifant!
       So the moment of truth had arrived...what would the so called
       wrong valve size combo give us...the answer was more
       power...everywhere. With 4 to 5hp more at 3 to 4000, peak torque
       rpm was next up...an extra 10hp & 4500 from the new combo wasn't
       to be sniffed at. With the old engine/head, power started to
       flatten out shortly after peak torque, but not anymore. With
       power now climbing much better than before we had an extra 12hp
       @ 5000, 13hp more at 5500 and peak was now 17hp up over the
       previous best @ 6K, with 127 at the wheels, around 152-153 at
       the flywheel, with power at 6500 10hp up too.
       With the car un-strapped from the rollers and a quick (quite
       literally!) run up the road completed, I brought the car back
       for Tim to try his new power unit....the grin on his face upon
       returning said it all.
       I feel there could be a little more to come as time didn't
       permit any inlet manifold/plenum porting at all, but for now
       Tim's 2ltr 8v is making the power it always should have.
       The graph shows the progress from as we first saw it, the
       tailbox change, and finally the current spec with the new head &
       improved squish & C.R.
       [URL=
  HTML http://s66.photobucket.com/user/mrhillclimber/media/Mobile%20Uploads/2014-12-11121101_zps8e428b75.jpg.html][IMG]http://i66.photobucket.com/albums/h278/mrhillclimber/Mobile%20Uploads/2014-12-11121101_zps8e428b75.jpg[/img][/URL]
       #Post#: 2165--------------------------------------------------
       Re: 2ltr 8v Digifant power
       By: Ganwinky Date: April 22, 2015, 4:55 am
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       We can work with others.
       #Post#: 2168--------------------------------------------------
       Re: 2ltr 8v Digifant power
       By: snowbopeep Date: May 6, 2015, 10:59 pm
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       A good topic to learn a lot. A very rich data The lot
       #Post#: 2180--------------------------------------------------
       Re: 2ltr 8v Digifant power
       By: toystoryful Date: May 25, 2015, 10:42 pm
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       I read a very good post here. Read I was able to use really.
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